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Project...Kahuna 66 cj6

Discussion in 'Builds and Fabricators Forum' started by bkd, May 11, 2007.

  1. Jul 29, 2009
    Patrick

    Patrick Super Moderator Staff Member

    Los Alamos, NM
    Joined:
    Sep 22, 2002
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    I should post a pic of my "new" blingy mirrors...
     
  2. Aug 1, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
    Joined:
    Apr 29, 2007
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    got the brake system finished yesterday.......the new booster had a threaded rod on the interior side, I needed to mod the old rod/fork to work with it. I cut it down and used a grinder to get it to the correct size then threaded it the match the new booster rod. Put a coupler on it and had it licked
    [​IMG]
    [​IMG]
    I finished up the install of the new saginaw box as well.......the pressure side hose drips a bit, guess I'll need to have it replaced eventually
    Took it out for a spin today.....it runs like a scalded cat :D............really looking forward to doing a run, but DD duties will suffice for now
    Jim S.
     
  3. Aug 1, 2009
    jeep peep69

    jeep peep69 Member

    redding ca.
    Joined:
    Dec 8, 2007
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    623
    that is good to here . Glad you got the bugs worked out and it is running right . have fun
     
  4. Aug 15, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
    Joined:
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    I went to a 4X show n shine last weekend that included 20 miles of freeway driving. I could not get the OD to engage so ran 65mph @ 3500rpm's.
    Wed. eve when I got home from work I had planned to pull it to see what was going on. Got out of the Jeep when I got home and saw antifreeze rolling out from under the front mehh. The fan had nicked the bottom rad outlet and I had a tiny spray......I pulled the radiator then decided to pull the OD, while under the Jeep I could see the trans cross member was loose no doubt contributing to the rad problem. The OD had a syncro that was messed up as well as a bearing damaged
    [​IMG]
    I ordered the parts to repair the OD from Herm on thurs. morning and they got here in todays mail :)
    [​IMG]
    Got everything put back together and installed the unit this afternoon.....(getting easier w/ experience)
    [​IMG]
    I decided to drop the radiator about 1" to give myself a little more clearance by the lower outlet. The old side mount wasn't gonna work anymore so I fabbed up some brackets to make a "saddle for the bottom of the rad to sit in. I used some material left from my winch mount plate
    [​IMG]
    I welded them onto my cross member so the rad could sit in them without being secured, and added some rubber strap under the radiator.....the rad can float so the flex won't tear it up
    [​IMG]
    [​IMG]
    All in all a good day....Od shifts well now, I'll put it through it's paces next week
    Jim S.
    OBA and the 8274 winch coming in the future
     
    Last edited: Aug 15, 2009
  5. Aug 17, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    devil is in the details.......I've been told by several people that I needed to shield the air filter from the hot air from the fan. They say it'll mess up the readings to the computer and cause performance issues w/ the 5.0.
    I started with a galv. sheet (probably 18g) and began cutting and forming, ending up w/ this
    [​IMG]
    I bolted it to the fender well so it'd block the direct flow from the fan
    [​IMG]
    [​IMG]
    guess we'll see how it works in the coming days :)
    Jim S.
     
  6. Aug 17, 2009
    Patrick

    Patrick Super Moderator Staff Member

    Los Alamos, NM
    Joined:
    Sep 22, 2002
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    8,360
    [​IMG]


    Dayum! You made a whole Lincoln!
    :D
     
  7. Aug 17, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    Apr 29, 2007
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    R)...hope the fender skirts I need to make for that boat go as well ;)
    Jim S.
     
  8. Aug 18, 2009
    willys59cj5

    willys59cj5 Sponsor

    Gilroy, CA
    Joined:
    Jun 1, 2005
    Messages:
    660
    Hi Jim, the build is lookin great. I have a comment on underhood air temps. As you know I run the megasquirt system and it has datalogging capabilities. After running the regular air intake that pulls air from underneath the hood temperatures were very high. The only way I was able to cool the intake air was to make a cold air intake that draws air from a source not directly under the hood. Hope this helps.
     
  9. Aug 18, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    Apr 29, 2007
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    so how did you accomplish that?......through the inner fender seems the only option
    Jim S.
     
  10. Aug 18, 2009
    willys59cj5

    willys59cj5 Sponsor

    Gilroy, CA
    Joined:
    Jun 1, 2005
    Messages:
    660
    I would say inner fender is the best option up high. I ran mine down towards the front crossmember as a temporary draw, but not good for crossing water holes:rofl:
     
  11. Aug 19, 2009
    sammy

    sammy Coca-Cola?

    Albuquerque, NM
    Joined:
    Jul 1, 2007
    Messages:
    1,577
    Dude snorkel it and call it good, real cold air intake! You know you wanna..... :twisted:
     
  12. Sep 6, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    my tires were rubbing the shocks at full turn in the front.....I didn't want to lose any turning radius so I removed the shocks and cut down the covers...
    you can see in the first pic how bad the rubbing was
    [​IMG]
    [​IMG]
    [​IMG]
    should help quite a bit....I checked for sag/compressed measurments and my bump stops and shock length are fine
    Still battling with clutch adjustment.....it's making a horrible noise on 1st gear launch
    Jim S.
     
  13. Sep 13, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    Apr 29, 2007
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    well I dropped the trans/tc today. I then pulled the bell housing and pressure plate/clutch. I found the problem
    [​IMG]
    the bolts on the flywheel were shiny as were the springs on the clutch....they were making contact and the noise. I took the clutch into napa so I could make sure the new one was gonna match. While talking to my buddy he asked what bolts had I used on the flywheel, I said the ones that came with the motor....he said the ones that were used for the auto flexplate?" yea I say those.....I then learned something new, the bolts from the flexplate /auto are differant (taller head) than the ones for a flywheel/manual :rofl:.....I purchased new arp bolts and the new clutch, tomorrows project
    I may have solved the motor problems I've been having as well.....found the cable that grounds the motor to the frame/battery disconnected....figure that may be effecting the sensors/computer:rofl::rofl:....keep your fingers crossed
    Jim S.
     
  14. Sep 13, 2009
    sdcj6

    sdcj6 Sponsor

    San Diego
    Joined:
    Sep 25, 2002
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    366
    Well if you had run it like I did they would have self clearanced in about 1500 miles.
     
  15. Sep 13, 2009
    fletcher0780

    fletcher0780 Member

    Connecticut
    Joined:
    Mar 27, 2005
    Messages:
    147
    :iagree:
     
  16. Sep 14, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    you two are funny.....it'd drive me nuts way before the "wear in"

    live and learn is my plight, or learn the hard way I should say. I replaced the flywheel bolts then went to work on the clutch. I could not get the trans/tc to index with the clutch, after half a day I pulled the clutch and checked the disc, it wouldn't slide over the input shaft of the tranny. Now I had checked the old/new discs at Napa to be sure they matched, but alas not close enough :rofl:.
    I measured the new 10" disc....10 spline 1/16".(standard Ford).....measured the old 10" disc/input shaft...10 spline 1/8".......we checked the books at Napa, even the Jeep T18 didn't match :(
    The solution was to keep the pressure plate and order a clutch disc from a 77 Olds ( 10" 10 spline 1/8")
    This jeep thing is a education that's leading me to the brink of insanity mehh
    Jim S.
     
    Last edited: Sep 14, 2009
  17. Sep 21, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    took awhile to get everything back together (kids busy schedules) but got it all buttoned up on Saturday. I drove my son across town this morning and then headed up to work, so far the clutch works great with no added noise :).
    The ground issue didn't clear up the engine glitch however. I dropped my son off then stopped for gas, motor running strong and smooth. Left the station and it began to stumble, not able to get to 2000rpm's. Came to a 4 way stop, proceeded and the motor was back to normal :?. Stopped at a 7-11 when I took off it stumbled again, came to a red light.....you got it, when I took off it was back to strong and smooth mehh:?
    Any ideas?.....thanks, Jim S.
     
  18. Sep 26, 2009
    bkd

    bkd Moderator Supreme Staff Member 2022 Sponsor

    K-Town Tenn.
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    good news, bad news, good news

    still having an issue with the motor performance. I pulled some plugs and they're all REAL lean...........
    1st good news, ........put a fuel pressure gauge on the fuel rail and drove around. Fuel pressure was betwwen 32lb and 40+ lbs, even when the motor was sputtering and back firing.........pump/system is fine
    2nd bad news........unplugged the plug to the air meter on the intake with motor running made NO change to idle :(.....wiring/bad ground/ or bad computer (computer is not throwing codes)
    3rd good news......without the air flow meter plugged in the Jeep runs like a scalded dog :D

    Got to get in touch with the mechanic who did the Mass Air swap, he's been stand up to this point so I think he'll take care of me.....stay tuned
    Jim S.
     
  19. Sep 26, 2009
    jpflat2a

    jpflat2a what's that noise?

    Hermosa, SD
    Joined:
    Jul 30, 2003
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    8,525

    :(
     
  20. Sep 26, 2009
    sdcj6

    sdcj6 Sponsor

    San Diego
    Joined:
    Sep 25, 2002
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    366
    Just take the mass air flow meter out, its just slowing down the airflow!
     
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